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This servicing took
place over Dec 8-18 at the Mimir Clean Room located on the first floor
of the Perkins Telescope building.
Present were Dan Clemens
and Brian Taylor, with consulting from Marc Buie.
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| Mimir
off telescope, on support cart |
Mimir,
with outer stainless steel cryostat cover and internal cold shield
removed, in clean room |
Areas and issues addressed
included:
Cryogenics/Cooling
During the period
September until warm-up in late Nov, Mimir was experiencing a lack
of adequate 2nd stage cooling, which prevented holding to the desired
33.5 K detector temperature. Many workarounds were tried during the
fall (purging, warming the helium shed) but none proved effective.
This period featured the "new" (used) DD-model CTI 1050
cold head. We sent the "old" CP 1050 off for refurbishment,
and expected we would have to install it into Mimir during this service
period. Instead...
1.
Test chamber put back into service
- Added
heaters and temperature sensors to the two cold stages of
the (just returned from refurbishment) CP 1050 cold head,
then installing the cold head in the test chamber, vacuum
pumping, attaching the helium system, and running the cold
head for a day.
- The
refurbished head failed to cool to proper operating temps
(it reached 112 K and 18K, instead of the 41K and 13K expected).
- We
did a complete flush/purge of the helium lines and compressor
and changed out the adsorber in the compressor.
- We
also did a complete flush/purge of the CP cold head (5 x
5 = 25 cycles)
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2. Cleaned up
DD Cold Head
- We opened
the DD Cold Head and found the 2nd stage ring seal, while intact,
was missing its backing split-ring spring. This was found to be
located up under the first stage displacer, along with the usual
ring seal cover (a full ring, not split). In August, the split
ring was put outside the ring seal when installing the cold head
into the SS cylinder in Mimir. This caused the split ring to slide
upwards and to not keep the ring seal pushed against the SS cylinder
wall. This ring seal failure seems to be the right explanation
for the poor 2nd stage performance seen all fall (while the 1st
stage seemed to work mostly normally).
- We cleaned
the displacers (ethanol soak, blown out with dry N2, then baked
at 60C in N2 atmosphere overnight), and reinstalled the DD cold
head into the SS cylinder.
- We purge/filled
with Helium (5 x 5 = 25 cycles) and ran it in the tests chamber
to recertify its operation.
- It produced
good no-load temps (41K and 15K) and a reasonable load curve.
3. Returned CP
cold head for repair
- With the
success in the test chamber of the cleaned up DD cold head, and
the similar failure of the CP cold head, we judged the CP had
failed acceptance testing and so sent it back to the firm that
refurbished it.
4. "Lecture
Bottles" removed from system
- Brian had
already found that our "lecture bottles" expansion volume
systems were leaking, so they were taken out of the system during
the late fall
- While we
had the DD cold head on the test chamber, we did an experiment
with and without one lecture bottle (on the supply side of the
cold head), finding no measureable improvement in cooling capacity
with the bottle.
- We concluded
that other than noise reduction, they had no benefit and would
no longer be in the helium system
5. Helium Gas
Operating Pressure
- Also while
the DD cold head was still on the test chamber, we experimented
with reducing the pressure of the supply-side helium delivered
to the cold head, looking for reductions in cooling capacity.
- This did
not occur until the gas pressure was lowered to 215 PSI, considerably
lower than the 290-300 PSI we had been operating at.
- We have decided
to henceforth operate at 245+/-10 PSI to provide adequate cooling,
but much better lifetimes for the parts in the helium system.
Filter
Wheel Interferences
| The
POL and FW3 filter wheels would once in a while stop rotating
while Mimir was operating. This happened because the clearances
between the filter wheel faces and the nearest bulkheads were
very small (32 mils, by design), the wheels carry some small warp,
and the filter wheel "stack" needed internal shimming
to set the wheel locations properly. From the previous warm servicing,
this amount was judged to be about 15 mils of additional shimming
between the stack that starts with FW3 and ends with the POL wheel.
Shims were designed to cover the inner portions of the axle bearing
races for the FW3 and FW1 wheels. This has the effect of pushing
FW3 "back" and the others forward, especially POL. The
shims were 12 mils thickness each. It did prove necessary to replace
the hex-head 4-40 screws that hold down the POL wheel position
encoding magnet blocks with button-head 4-40 screws to remove
a *new* interference introduced between these screws and the back
of the collimator. Once the screws were replaced, the POL wheel
turned freely with no interference. |
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| After
rebuilding the filter wheel/axle stack, and reinstalling into
Mimir, no interferences of any kind were found in the four filter
wheels. All turn easily both directions and for all filter locations.
The filters were reinstalled (with 3 unfinished filter cells added
in FW2 and FW3 to improve balance) and the full systems tested
in both horizontal and vertical orientations of Mimir. All wheels
worked fine, all encoders worked fine. |
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Slit/Decker
Unit Upgrades
| The
slit/decker unit has not been working reliably or accurately for
the past two years. The problems were: (1) inability to reliably
position the slit or decker to the same location in the beam,
(2) drift of the slit with hour angle by about 1 full slit width,
and (3) slow maximum speeds of the slit and decker car motions. |
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1. Positioning
reliability improvement
- We believed
that the positioning problem likely stemmed from the nature of
the deep pin-based detent unit attached to each stepper motor
- A new detent
system was designed to run on the drive screws instead of on the
motors
- Parts were
fabricated, some anodized, and were installed on the slit/decker
unit
- The detent
forces were tuned, and the detents sensed using reed switches.
- These systems
(one for each of the slit and decker drives) seem to produce somewhat
smoother motions and allow higher step rates (by up to a factor
of three or so).
- The old motor-based
detents were removed from the unit.
2. Slit sag improvements
- Examination
of the drive systems identified four places where play could introduce
slit wander or sag
- The first
of these places, namely the motor gear to drive screw gear mesh,
was measured and found unable to contribute enough motion to explain
more than 1/10th of the slit motion. Also, with the new drive
screw detents, this gear mesh is no longer "down stream"
of the detent, and so will no longer contribute any slit motion.
- The second
place is in the drive screw "nut" that captures the
rotating drive screw and turns it into car motion. However, this
nut is comprised of a set of recirculating ball bearings, with
many in contact with the screw threads at any time. Pushing on
the nut unit developed no more than 1 mil of relative play, and
so was judged unimportant (the slit wander is some 7-10 mils).
- The third
place is in the bearings and springs used to locate each drive
screw relative to one end pilon for each of the slit and decker.
In fact, the decker drive screw was essentially floating free
along its length, though the slit's drive screw was not. This
was fixed by adding additional wave washers to the end of the
decker drive screw that captures these wave washers between a
flat washer and one shoulder bearing in the opposite side end
pilon. After this tuning, both decker and slit drive screws were
judged well located and fixed to 1 mil or better.
- The fourth
place where play was evident was in the slit and decker cars themselves.
Both showed strong torsional motions - the ability to twist about
the single bearing race holding their "tops" on one
steel rod.
- We
measured the importance of this torsional motion
by attaching a dial indicator to the baseplate,
then indicating off the side of the slit car.
- When
the unit was rotated to simulate different hour
angles on the telescope, the dial indicator showed
linear motion of the order 7-8 mils, right in line
with the wander of 1 slit width seen on the telescope.
- The
cars are held onto the two opposing steel idler
rods via sets of recirculating linear bearing units,
themselves held to the slit and decker cars by C-clips.
- However,
the linear bearing units had some play with respect
to their cars.
- Shim
washers were made and installed between the C-clips
for the linear bearings and the cars.
- This
cured the torsional motion problem enormously. We
reperformed the dial indicator experiment, recording
a maximum motion of 2.5 mils at the end of the car
farthest from its drive screw. This should translate
to under 1.25 mils of motion of the slit center.
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Close
up, pumping
Mimir was closed
up on Sunday, Dec 17, and pumping with the new scroll pump started.
About 24 hours later, with the dewar pressure about 0.120 torr,
the turbo pump was added and run in "standby" mode (low
RPM) until the pressure was below 0.050 torr when full RPMs were
allowed. The pressure fell to 1 micro-torr within a few hours. During
all this time, the cold bulkhead heater was on, to drive that part
up to 320 K (under closed loop control) to aid in getting water
off the anodized surfaces. This bakeout will cease after 48 hours.
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